Ok, I have installed a new OS, file name Erle-Brain2-PXFmini-RaspberryPiZero-frambuesa-12-10-16.img. I managed to get Mission Planner connected and then perform all mandatory hardware configurations, including claibrating the RC.
But, when I tried to calibrate the ESCs the PXFmini did not perform as expected. This is the procedure I followed.
1. Turn on radio and push throttle to high position.
2. plugin battery until lights flash like an ambulance
3. Unplug battery then plug it back in.
This is where things went wrong. The orange and green LEDs were light solid.
4. I tried repeating the calibration process 3 times with the same result each time.
I did a quick launch of the quadcopter to see if it would fly. It lifted off up to 1 meter high and was spinning rapidly so I landed it quickly and disarmed it.
Could you help me with how to go about troubleshooting this problem. Do you want to see logs from the test flight or from Mission Planner>