I set the following parameter, but I noticed today that the cpu averaged around 50% today. So should be good.
This makes sense that it is normal behavior, since I never see an error when it disarms.
The issue is I have not gotten it off the ground yet. I have not been able to arm the drone with the TX (I am using a Turnigy Evolution with the TGY-iA6C reciever). I have no trouble binding the TX to RX. But it does not register when I try and calibrate the radio.
I receive an error when running the Radio Calibration through APM Planner v2.024: "Radio Control is not active or turned on". I assumed this referred to the TX itself and that it's not recieving any signals. Could it be referring to something else?
Also, can you provide the process to arm the drone. I've read through the instructions a few times, but at this point; either, I've been doing something really stupid (and wrong) or the hardware is defective.
P.S. I was fooling with some settings and have it hooked up the the monitor. Now when I turn it on, I hear 4 beeps; 1sec long and about 2sec interval. Haven't heard it before. Any idea what it is?